Entries in gearhead (2)

Monday
May292017

#SaveEddie, Part I: The Coefficient of Friction

Summer tires are a fine thing for driving. When I talk about my seasonal tire strategy, I’m often confronted with the inquiry, “Why don’t you just use all-season tires?”A part of me wants to tell them they’ll never understand. However, years of working in the service industry has trained me to temper my snippiness. Instead, I’ll illustrate that four-season tires are a compromise that results from convergence.


I’ve observed for many years that when the features of two products are converged into a single unit, the merits of these features always become compromised. The most successful convergence to my mind is none other than the Clock Radio: take a standard tabletop radio, glue on a digital clock, and interconnect the two such that the radio can be turned on at a specified time. Low and behold, it works! You set the trigger to five minutes before you head out the door for work in the morning, and sure enough the radio turns on at 7:55 A.M., thus waking you to the sound of morning talk show antics. You stir, looking for the source of the noise and see the current time displayed on the chronograph. Your half-asleep brain does a bit of arithmetic, then fires a surge of adrenaline through your body to get your lethargic ass energized to shower, shave, dress and sprint out the door while praying a power outage scrambled the time clock at work last night so you can slip into your office undetected by the higher-ups.

 

The Clock Radio works as advertised, even if your body clock doesn’t. However, you probably aren’t listening to Sublime’s new single on this thing. No, you want the good stereo your older brother bought with money from selling midterm answer sheets, don’t you? So, while the Clock Radio is a perfectly functional clock paired with a perfectly functional radio, it failed to exemplify the best attributes of either product. Sound quality is rather limited, given the single speaker. And, for many, many years, it wasn’t a particularly attractive clock, never destined to hang upon the wall alongside Great-Uncle Charlie’s self-portrait.

 

And so, we have the all-season tire: functional in summer, functional in the snow, but failing to match the potential in either when asked of it.

  Summer tires can’t cut into the snow because the tread pattern is meant to displace liquid water rather than powder, while the knobbly tread on a snow tire allows for some flex, meaning decreased grip in dry conditions.  As such, many drivers elect for a best-of-both-worlds approach, and have the dealer bolt on four all-season tires, and they won’t have to worry about it until they wear out.

I take a different approach.  Last year, I purchased a new set of rims and had some Bridgestone summer tires installed on them. I took off my stock rims, which had winter tread on the front axle and still-good all-seasons on the back, and bolted up the new ones for a transcendent experience in traction. These tires provided me with a spirited driving experience all through spring, summer and fall, until early December when I switched them back. Some may see the twice-annual change as an inconvenience not worth having, but I consider it time well-spent for an engaging driving experience nine months out of the year and peace of mind during the other three.

Back to squishy, cold weather compound for a few months, which brings me to late February.

Conditions were moderate in temperature, but high in humidity due to earlier rainfall. Much of that moisture was still on the asphalt as I crested a hill to find someone stopping quickly to turn left off the busy street. The duty then fell to me to modulate braking pressure to avoid a lockup. Normally, the anti-lock brake system’s computer would do that for me, but thanks to a break in the wire leading to the front-right wheel sensor that I haven’t been able to chase down, my ABS is inactive. Locking up the brakes would be bad for me, since I have moving traffic on my right, while there’s oncoming traffic to the left, and if I were to spin it would be far worse than unfortunate.

So modulate the brakes I do, and I can hear these winter tires howl like a wounded animal; a sound generated by combining the flex of rubber under stress with turbulent airflow around the tire’s tread. My heart stops, hoping to inspire the car to do the same, but it isn’t enough in these greasy conditions to prevent Eddie from colliding into the back of a late 2000’s Nissan Sentra.

 


Thursday
Jun192014

LeadFoot Video: Oil, Wind and Fire

I take pride in my car.  A 1999 model year Pontiac Sunfire sedan with a 2.2 liter engine, 3-speed automatic transmission with overdrive, aftermarket radio and tasteful body-colored rear spoiler.  I call him, “Eddy.”

Sure, it’s fifteen years old.  Sure, we got it just before GM canned the Pontiac brand.  Sure, it hasn’t got much power, it shakes the front passenger door panel when the compressor’s on, someone in the parking lot at work put a big dent in the rear driver’s side door, and it’s not great on gas (despite its four-cylinder engine; damn the three-speed auto).

But beyond all this, I love it.  The car has grown on me these past five (almost six) years.  In that time, much has been done.

Before we even got it, it had been in a front-end collision.  This was immediately apparent, because the front passenger door doesn’t fit right in the frame and generates significant wind noise at highway speed. In addition, the plastic bits in the front-right wheel well aren’t in good shape, and rub against the wheel in full-left steering lock.  This became gloriously apparent when a bolt on the water pump wore a hole in the coolant hose, and half a dozen pieces of plastic had to be removed to attach a new hose (with proper screw hose clamps and the old hose wrapped around the new one for protection.

Actually, now that I’m thinking of it, I should probably investigate that hose.  It has been a while.  Next time.

If I recall correctly, the next thing we did was regular maintenance (brakes and the like).  There was a coolant temperature sensor that went bad, which made for some interesting readings on the dash.  And almost three years ago, we found the starter motor was going.  The OBD reader was throwing off some weird codes because of the voltage drop on that occasion.  Replaced that part in a parking lot.

Then two years ago, the air conditioning died.  In the middle of summer.  After an entirely new system was installed, we eventually we’d found that multiple slow oil leaks had worn out the rubber bushings in the torque strut mount, and without the dampening effect of the mount, the engine was rocking forward, rubbing the AC hose on the radiator fan grille, rubbing a hole in the line, allowing Freon to escape.

Replacing the mount would have been cheaper than rebuilding the engine (the ultimate solution to the problem), and we had a warranty on the earlier AC system work, since we were at the same shop, so we had them install a new mount and they’d replace the AC line for free.

(Between this and the next service, the cooling fan motor had gone, which was an interesting day in and of itself, and I shall detail it another time.)

To their credit, when they did the complimentary AC work, they’d wrapped the line with rubber hose, like one from a coolant system, and zip-tied it on.  This was very kind of them, and I’ve always respected them for this.  But in practice, rubber is a soft material, and if you beat on it enough times even with plastic, it will be eaten away.

Lately I haven’t been driving as much, living so close to work, so I haven’t been able to notice the recurring problems with the Sunfire.  As summer has been rolling in, I’ve finally noticed the air conditioning wasn’t working again.  This meant another possibly damaged hose.  I watched the engine as I shifted from neutral to drive and reverse, and saw that dramatic rock-forward as the transmission shifted into reverse and the engine pushed against the torque converter, pressing the AC line on the radiator fan grille, rubbing in that ever-irksome hole in the system through the rubber covering.

Upon learning this, I immediately banned myself from using reverse gear to prevent further damage.  This meant I would be walking to work more often (especially because the scooter has decided to go on strike; All this time I thought it was Chinese, turns out it was French).  It made it interesting when I had to back out of my parking space at home, and there’s a big column on the driver’s side that would have hit the door, so I was pushing from the passenger side and hoping the steering would stay straight.

One day, I was running too late for work to walk, so I braved driving.  Sitting at an annoyingly long light, I saw the engine temperature climbing uncomfortably high.  Oh, crap, there goes the cooling fan again.

So to sum up so far, we’ve got no AC, no reverse, and no cooling without forward momentum; a veritable trifecta of problems.  I’d guessed I’d need a whole day to resolve them.

So finally comes a day off from work, and I get down to business.  Quick trip to [insert national auto parts store here], and I had a torque mount, cooling fan motor, some engine degreaser and a headlight polishing kit.

Let’s get this out of the way: I’ve seen the results of those kits that involve just wiping the oxidation away.  Do yourselves a favor and use a kit that needs a drill.  It’s just better.  Eddy’s headlights are sparkling now, and they light up the end of the street.

With the car on ramps, I doused the oily bits with engine degreaser and followed it up with a spray from the hose.  It did all right, but there’s so much caked-on oil, I’d need a stronger product.  In the meantime, elbow grease took care of the worst engine grease, especially around the torque strut brackets.  They’re nice and clean now.  Or, at least, they will be for a little bit before oil gets on them again.

Removing a torque strut mount is a simple affair: wedge some plastic parts out of the way and loosen the two bolts, letting the mount fall free.  One normally has to loosen the bolts about an inch and they can be pulled out (there’s only thread on one side of the bracket, and not in the torque strut itself).  Such was not the case.  As soon as the bolt was free of the thread, the engine pulled on the strut, holding the bolt at an angle so I had no choice but to unscrew it the entire length.  The front bolt, having more play, took on some especially interesting angles.

At last, it was free and I could further clean the grime off the brackets.  Then came time to put in the new one.  Rear bolt in: Check.  Front bolt in: Um, the bracket’s not supposed to be that far away…

The engine had shifted forward almost two inches, and my arm strength from underneath the car was not enough to force it into place, let alone hold it there while my other hand inserted the bolt.  A super-strong, eighteen-inch screwdriver employed as a pry bar couldn’t give me the necessary leverage, either.  I had a ratchet strap in my trunk, and I was able to find two suitable points for the strap, but it was such a piece of [expletive] it couldn’t even move the engine half an inch without slipping.  And every time it did slip, it did with such force and noise I thought the world was going to end.  I’m amazed my heart’s kept beating to this day after seeing all that.

It’s worth saying now, I think, that I had taken the car to my parents’ house.  My lease prohibits automotive repair done in the garage (though I’ve done quite a bit to the scooter there), and my dad had a set of ramps I could use to raise the car.  (They’re old, so I put some blocks of wood underneath them for peace of mind, as I’m not fond of 3000 pounds of metal landing on my face, but they held up all the same.  Good job there.)  There’s also a power drill for the headlight polishing, a hose for the engine cleaning, and a much shorter walk to a refreshing drink of water.  It’s been kind of hot lately.  The house also has a backup vehicle in case I needed to make a run to the national chain parts store.

My folks are on vacation, having taken the minivan, because it’s better at carrying many things.  My dad’s car is a Honda subcompact with a manual.  His old car is a Nissan subcompact with an automatic, which my sister now drives to her work.  She was home while the folks were away, just hadn’t gotten home until I’d gotten to the torque strut part.

Having realized manual labor and a lousy ratchet strap wouldn’t be enough to move the engine, I knew I’d need to make an additional purchase.  An educated guess told me Harbor Freight should have something.

Side note: This mention of Harbor Freight is an actual endorsement.  I’m not being paid for this, I just think it’s a great place to buy that one tool you need for that one occasion you didn’t have a tool for before, and probably won’t need again, and getting a decent price on it.  That said, it took a while for me to find what I was looking for.  In my head, I was looking for a bigger, badder ratchet strap than what I had, but ended up with a steel cable ratchet that was hiding in the “Trailer Hitch” section.  I was thinking it would have been in the “Rope” section, which didn’t exist in the first place.

An earlier Skype conversation had granted me permission to use the Honda if need be, so when I’d come to the decision to go to the store, the only thing in my head was, “Okay, I’m going to borrow the Honda, get the part, and be back before the dinner my sister cooked gets cold.”  My sister was home, as was the Nissan, but still it wasn’t until I got to the second main street after a couple of hard shifts before I asked myself, “Why didn’t I take the AUTOMATIC Nissan?”

But as a gearhead, I was already committed, and in my defense, it was only the fifth time I’d driven a stick-shift. So a couple of rough shifts and two stalls on uphill starts later, I’m back with a cable come-along.

Used in conjunction with the lousy ratchet strap (which works better at shorter lengths, and adds length to the new steel cable ratchet), I was able to move the engine into place and hold it there to screw in the bolts (which are, thankfully, thick enough to withstand the forces involved).

Much cursing and grinding of teeth got me this far, and the sun was going down, so something involved as replacing the radiator fan motor would warrant checking simpler solutions first.  So, multimeter in hand, I disconnected the fan motor cable and pulled the coolant temperature sensor connector, forcing the fan to turn on.  Sure enough, the car’s computer wasn’t sending the necessary 12V to turn the fan in even the worst of circumstances.  This meant there was an electrical problem bigger than the motor, which I didn’t have time or resources to diagnose. So I called it a day, feeling I’d at least accomplished three of my four goals.

The fan motor turned out to be a bad fuse upon another trip to the national auto parts chain store.  While I was there, I grabbed an air conditioning system stop-leak product, along with a recharge kit.  Hell, it’s worth a shot, right? And if it works, it’s better than half-a-grand in shop repair.

So here we are, in the end, I have a new torque mount, clear headlights, and (kind of) clean engine,  a working fan motor, and a (for now) working air conditioning system.  I’ll call it a win for at least two weeks.  Beyond then, Eddy probably needs AC work…